Page 2 of 3 FirstFirst 123 LastLast
Results 16 to 30 of 31

Thread: radial arm saw has 20 thousandths of wobble in the blade

  1. #16
    Join Date
    Dec 2011
    Location
    Lexington, Oh
    Posts
    509
    One other thought... the outside blade washer should be the same diameter as the inside one. If not, or if you don't have the outside washer, tightening the nut can really distort the blade! Just a thought.

  2. #17
    Join Date
    Sep 2009
    Location
    Midland MI
    Posts
    887
    There is an outside washer. It's just not in the picture, they are the same size

  3. #18
    Join Date
    Dec 2011
    Location
    Lexington, Oh
    Posts
    509
    Cody, what's the model of that saw? Did you try exchanging them?
    Last edited by Duane Meadows; 11-21-2014 at 9:59 PM. Reason: My typing is worse than my spelling!

  4. #19
    Join Date
    Mar 2003
    Location
    Upland CA
    Posts
    5,557
    The washer in your pic looks like a stabilizer accessory to me, Cody. Check the online manuals for your saw, and see it that is what the arbor washer is supposed to look like.

    Is it steel?

    Rick P

  5. #20
    I have two ideas, neither of which may be relevant. 1. Is the motor/blade exactly perpendicular to the table and is it exactly perpendicular to the fence? 2. Try a 4" blade stabilizer.
    Mike Null

    St. Louis Laser, Inc.

    Trotec Speedy 300, 80 watt
    Gravograph IS400
    Woodworking shop CLTT and Laser Sublimation
    Dye Sublimation
    CorelDraw X5, X7

  6. #21
    Join Date
    Jun 2006
    Location
    The Hartland of Michigan
    Posts
    7,628
    I can see this whole thing going south.
    Cody, find someone that knows machinery to help and advise you.
    Never, under any circumstances, consume a laxative and sleeping pill, on the same night

  7. #22
    Join Date
    Mar 2006
    Location
    Austin Texas
    Posts
    1,957
    As Duane said, did you check to see if the wobble you have exists in the motor shaft? This needs to be done first before you chase a problem that is not the real problem. If the arbor is OK, then you will either have to try and flatten out the flange washer on the saw or off the saw. Without being there, it would seem to me that removing the arbor flange from the saw and spinning it down against a stone would be easier (paint the surface with Marks-A-Lot to check on progress). Or, use some spacer washers and a nut to hold the flange tight against the arbor for truing in that fashion. You may have to grind down some washers and another nut to expose enough of the outer rim of the flange washer to push the stone against. At some point, you will need to try something.
    David

  8. #23
    Join Date
    Dec 2011
    Location
    Lexington, Oh
    Posts
    509
    Put a mark on the arbor, and a mark on the washer. Turn the washer 1/8th of a turn reinstall blade and recheck the runout. Do this for a full turn. If it follows the washer, the washer is the issue. If it stays in the same position relative to the arbor, then the arbor/arbor bearing surface is the issue.

    Being that the washer is removable, flattening it off the saw would be much easier. Both surfaces of the washer need to be parallel(perpendicular to the arbor hole as well!). Work carefully! It will likely require removing only a very few thousandths of an inch from the high side. Marking as above will help in determining the where that high spot is!

    On my saw the inner and outer are very similar, if not indentical. Thus I would reverse them and check the runout again. If it decreases, pretty good indication the inner washer is at fault!

    Myk, it really ain't rocket science! I spent 30+ years as a tech for Sears. Have worked on many a RAS over the years.


    Also, though very important, blade alignment to the table, the arm, or anything else will not cause blade runout. It will of course cause quality of cut issues!

  9. #24
    Join Date
    Sep 2007
    Location
    Reed City, MI
    Posts
    31
    Is the hex spacer loose on the shaft. or fixed? Before I did any grinding, I would assemble the blade, washer, and spacer on the shaft, then make a mark on all three so that alignment can be duplicated. Check the runout and mark the outside of the blade at it's highest point. Then alternately rotate each of the 3 components 180*, checking runout with each configuration. This should tell you which component is out of whack. Long story short, if you grind away on the washer and it was the spacer or blade that was bad, you'll have the same problem unless all the components are aligned the same every time you put the blade on.

    Come to think about it, I would add the shaft to the list, making it 4 components as variables.

    Paul
    Last edited by Paul M Miller; 11-22-2014 at 1:20 PM. Reason: Addition

  10. #25
    Join Date
    Sep 2009
    Location
    Midland MI
    Posts
    887
    I worked on it today, got it down to 8 thousandths wobble then ran out of time will try for better tomorrow, what is acceptable for this?

  11. #26
    Join Date
    Aug 2011
    Location
    PALM BAY FL
    Posts
    515
    Quote Originally Posted by cody michael View Post
    I worked on it today, got it down to 8 thousandths wobble then ran out of time will try for better tomorrow, what is acceptable for this?
    That is a personal preference, anywheres from 0.0" to .008", depends on what you deem acceptable- the real test is to make a shallow kerf in scrap, compare it to the blades' tooth width. Good work though, once you took the plunge it wasn't all that bad now was it?
    - Beachside Hank
    Improvise, adapt, overcome; the essence of true craftsmanship.

  12. #27
    Join Date
    Sep 2009
    Location
    Midland MI
    Posts
    887
    It took a little while to figure out good technique but is going ok, my biggest issue is there are still saw marks on my endgrain.

  13. #28
    Join Date
    May 2009
    Location
    Boston
    Posts
    1,740
    Have you gotten a copy of the manual and set the saw up?
    Don

  14. #29
    Join Date
    Sep 2009
    Location
    Midland MI
    Posts
    887
    I really need help, I have spent 5ol or 6 hours working on this over the weekend. At one point I had it down to 8 thousandths but I still was happy with the cut, I tried to get it closer and made it worse, it is now about 25 thousandths, of wobble. I really like this saws setup.

    Can someone please let me know if there is something else to try or if I can get a new arbor? Or do I just need to look for a new saw? The blade on start up wobbles enough you can see it. I am somewhat mechanically handy but have never had an issue like this


    I think part of the problem is the inner arbor washer isn't fixed in place, it just hits a small nut shaped spot. I think if that is off a hair or the back of the arbor is off then when it spins it throws everything off. Otherwise I don't understand how grinding it down doesn't fix it. I start with the grinding stone just hitting the high points let it run for awhile. Tap it a little closer let it run do that a few times then when it seems to not have high points I check it with dial indicator. I haven't been able to get the arbor washer to have better then 2 thousandths run out. I'm very frustrated

  15. #30
    Join Date
    Apr 2003
    Location
    Birmingham, AL
    Posts
    335
    post some good close up pictures of the arbor and the washer and nut

Posting Permissions

  • You may not post new threads
  • You may not post replies
  • You may not post attachments
  • You may not edit your posts
  •